Well, I would be lying if I said that getting the chassis running with all the motion fitted was anything but a trial. Much of it my own doing. I am not sure how but I had scaled the drawing wrong so my many attempts were all destined to failure I just didn’t know it yet. It was mention of the scale size of one of the rods that Ian Allen @lancastrian) posted on the Guild forum that made me double check and find the error. A trial assembly of the final version of the return cranks confirmed that they were indeed almost a millimetre too long between centres.
I confess, that this almost did me in and I nearly consigned the 8F to its box for another decade. Saner heads prevailed and I recalled the drawing, redrew the return crank in Fusion 360 and created an updated working drawing. From there I made a ninth set of return cranks and again I made an error in so much as I predrilled the cranks and the small bosses that I added to clear the ends of the studs protruding above the face of the crank. When I then soldered them together, I hadn’t noticed that the holes were slightly out of line until I tapped them the tapped them and the tap went in at angle. So, I started again and this time I made four return cranks with the view that I could pick the best two.
This was taken part way through making them. – I did trim down the boss on the deeper pair after testing.

Having taken great care in the shape of them I also only drilled a pilot hole in the bosses. Then I clamped the cranks to my Metalsmith drilling plate in the mill vice and drilled right through to ensure that all the holes were aligned.

Next, I used a small engineers clamp to clamp the cranks to my tapping jig to ensure that the tap was aligned to the hole and then they were tapped 12 BA


I also used my homemade tap spinner to reduce the risk of breaking the tap.
Finally, I had two pairs of cranks fitted with miniature studs

A test fit had me heaving a sigh of relief as they fit and the motion turned over under power but there were a few clicks where the bits were catching. I knew that clearance was always going to be tight so I patiently worked my way through the various parts easing them.
They included but were not limited to, filing two etched bolt heads off of the insides of the expansion links; filing the bottom front corner of the new valve blocks to allow a minute amount of extra forward travel; turning the head of the 14ba steel screws that retain the combination lever to the valve block down to the thread thickness while retaining the slot, to allow them to be easily removed. Again, to allow a minute amount of further forward travel; easing the faces of the connecting rods to allow the expansion link to pass without catching. – Incidentally I measured the thickness kit provided connecting rods at 1.7mm and the Premier ones at 1.5mm so had I used the kit rods that problem would have been exacerbated.
I also replaced a couple of 14ba brass screws (which retain the expansion links) with some homemade nickel silver replacements with the view that they would be slightly more hardwearing than the brass ones. In fairness given how little mileage my locos actually do. this may have been overkill on my part.
After all that I had a smooth-running chassis. The tinging noise that you can hear is because I haven’t permanently fitted the retaining pins that hold the radius rod and the combination lever together yet so there is a bit of slop in them.





































































