The day before leaving for Stafford I had a bit of a disaster with the motion on the Princess in so much as one of the combination lever’s snapped off while it was running on the rolling road. Initially I thought that it was due to there not being enough material left after opening out the holes for the locating pins but once I got back from Stafford and was able to remove the top end (the simple task of unscrewing a couple of 14ba screws) I found that the rod had actually snapped part way down the fluted section. I think that I have just been unlucky in that it was over cooked etch wise and that there was very little material left. there is so little that I cannot get my camera to focus on it to show what I mean.
Thankfully I had a couple of spares courtesy of Nick Dunhill so I have prepped a replacement. Not taking any chances on this one I have soldered a small strip of 10thou (0.25mm) onto the back of the rod to add a little extra strength. This has been done in fits and starts because like many other Chris and I picked something up at Safford that has taken a bit of shaking off. We have started to feel better one day only to feel crap again the next. Fingers crossed it’s behind us now.




I just have to refit it to the loco now.