Fitting a Digital ReadOut (DRO) to My Sieg SX1LP Mini Mill Part 5

The X axis was a bit more involved in that it was harder to get access to even with the mill unbolted from the bench.

First job I found that the slots in the mounting plate were a bit tight for the M5 screws so I opened the slots with the mill.

I also milled the second slot to have vertical as well as horizontal movement as it’s important to have the scales both level horizontally and parallel to the travel of the table for the highest accuracy. As they come one slot is vertical and the other horizontal but being aluminium they are easy to modify with the mill.

After bluing up the rear face of the table I was lucky in that I had recently bought a couple basic C clamps to use for clamping one of my vices and my rivet press temporarily to the workbench when I need to. These fit quite nicely edge on in the T slot so I was able to clamp the mounting plate in position allowing me to move the table to either side of the column so that I could mark it up without removing the table at this stage.

Again, it was a bit of a squeeze but I was able to drill and tap the table without removing it.

The next task was working out how best to mount the reader but I will cover that in another post.

Fitting a Digital ReadOut (DRO) to My Sieg SX1LP Mini Mill Part 4

The next step was working out where to position the reader to get the full length of travel from it. I measured how much space the X axis scale would take up when fitted, added a couple of millimetres for clearance and used that as my forward limit. I then marked the base and drilled and tapped the base.

This is the Y axis scale fitted with it’s swarf cover and working.

Fitting a Digital ReadOut (DRO) to My Sieg SX1LP Mini Mill Part 3

I mentioned that I started with the Y axis first

There was a convenient ledge on the side of the bed casting which allowed me to add a parallel to get the backing plate up to the right height to mark for drilling the mounting holes. The 123 block is just holding it in position.

I added some engineers blue and marked the holes with a scriber then punched the centre.

Drilled, tapped and cleaned up with IPA

The backing plate in place, so far so good.

A trial fit of the scale to work out where the reader needs to be fastened to.

At this point I realised that I would need some packing pieces behind the mounting plate to make it stand off due to the useful ledge that I referred to earlier and allow the reader a clear track without being forced to run at an angle and to allow the fitting of the chip shield which didn’t quite fit when flush against the table.

I used a slitting saw to cut down some sheet material which some bar stock had been attached to to stop it being bent in the post. It’s quite interesting material in that it is two layers of thin aluminium bonded either side of some plastic material. Being layered it’s remarkably strong and light and I thought it too good to throw away so it went into my useful bits box.

You can just make out in this shot where I slotted the vertical mounting holes in the angle bracket, again to allow the reader to track without adding undue pressure. You can also see the packing strip between the mounting plate and the edge of the table.

Fitting a Digital ReadOut (DRO) to My Sieg SX1LP Mini Mill Part 2

The Warco items duly arrived and each scale, came with a main rear mounting bracket and a pair of additional mounting brackets (Shown below) and a selection of M4 and M5 cap screws.

Main mounting bracket.

Warco Glass Scales Mounting Brackets

These are the additional brackets that were spare as I only ended up using one of each along with some sections of aluminium angle which I had rescued from a set of shelves that I had dismantled.

To ensure that the job wasn’t stopped for lack of drill bits if I broke any, I put in and order to Drill Services Horley for a couple of 3.2mm and 4mm drill bits. Of course because I had them to hand I didn’t break a single drill bit.

All the holes drilled in the mill itself were done using a battery hand drill and being cast iron it was quite easy going if a bit messy.

The main mounting bracket holds the glass scale and then the read head is mounted so that when either the read head or the scale moves it reads off the distances. In my installation I have the scales mounted to the moving table axis and the read head’s fixed to the machine bed. On the Z axis this is reversed and the scale is fixed to the column of the machine and the read head moves up and down with the milling head.

I decided to start with the Y axis as being one of the shorter ones so easier to handle and definitely the easiest to access on the left side of the machine. However as soon as I took the 100mm scale out of the packaging I knew that I had made a mistake in getting a second 100mm scale for the Z axis although it would be fine if I was working with the vice or rotary table mounted on the bed it wouldn’t allow the head to come down far enough to mill anything directly mounted to the T slots of the table.

I immediately contacted Warco and explained my error and asked that since I hadn’t opened the second scale, would it be possible to return it, and swap it for a 200mm scale. They were happy to do so and would sort out any additional cost incurred once they had it back with them. I returned it to the address on the signature of the person who had sent the invoice. This proved to be a mistake as it turned out that they had moved from that address so the package was returned to me. I called them and advised that there would be a delay due to my sending it to the wrong address which was on their email.

I looked at the actual invoice and noted their new correct address and re sent it there. As good as their word they very quickly despatched the replacement and didn’t charge me a penny which despite my frustration at them not having the correct address on their correspondence I did appreciate.

Fitting a Digital ReadOut (DRO) to My Sieg SX1LP Mini Mill Part 1

For my birthday last October I received a Digital ReadOut (DRO) kit for my Sieg SX1 LP mini mill. I fitted it over a weekend last October and although I took photos as I did each stage, I haven’t yet got around to writing it up. Paul’s posts (@OzzyO) on fitting a DRO to his mill prompted me to get my finger out so that anyone who is interested will get a couple of takes on fitting them to different types of mill.

As I am not anywhere in the same league as Paul when it comes to machining, my first port of call when looking was to YouTube. To see if anyone had done a video on fitting a DRO to a similar mini mill. I was quite surprised that at that time there wasn’t any to be found (there may well be now as I haven’t looked since).

Having realised that I was essentially on my own, my first port of call was to ring Arc Euro Trade whom I bought the mill from. To ask if they did a DRO kit for my mill. I was a little surprised that they didn’t, as they seem to cater well with other accessories and tooling for the range of machines that they sell. Their recommendation was to talk to a company called Touch DRO who apparently do something suitable.

I have seen a few videos which featured Touch DRO units and confess that I was not keen on the idea. This is on the basis that they require the use of scales, which connect via Bluetooth to a tablet for the display. I spent 20 years in IT support and the last thing I want is yet another device.

Again on the basis of seeing a few videos on badged variants of the units supplied by Warco I opted to buy from them. I got a display reader, two x 100mm glass scales and one x 250mm.

The idea was that I would use one of the 100mm scales on the Y axis (front to back movement of the table for those unfamiliar with the axis terms) and the other for the Z axis which is the up and down movement of the mill head. This latter proved to be a mistake which I will elaborate upon later. The 250mm scale was to be used on the longer X axis table (which is what the LP designation of the model number refers to).

Slaters SG38CANL Gearbox – Something you need to know when buying one

Although I didn’t go to Kettering I did receive a Slaters SG38CANL Gearbox which had been bought at the show for a little job that I was asked to do.

Slaters SG38CANL Gearbox
Slaters SG38CANL Gearbox
Slaters SG38CANL Gearbox

Although I haven’t fitted it yet I foresaw no real problems until I was looking at the final drive gear and the grub screw that retains it. This is something that I pay attention to as I have been bitten before and indeed this one is a replacement for one of the former San Cheng gearboxes which required a slot cutting in the axle to allow the grub screw to screw in far enough to clear the intermediate gear above it.

Slaters SG38CANL Gearbox

Although this image is much magnified, the grub screw fitted to the gear is tiny and I had no idea what size hex key it needed and no way of measuring it. I decided to give Slaters a ring to ask what size I needed.
I rang and explained my problem and the gent that I spoke to (Martin) immediately said Oh! we should have supplied one, let me have your details and I will get one in the post. He was good to his word and from a call at 1pm on Thursday I had the hex key delivered on Friday lunchtime.

For anyone who find themselves in the same position or loses one, the size is 0.9mm

Homemade Needlepoint Oiler

Like many modellers, for years I have had one of those cheapo plastic Needlepoint oilers that are available via Amazon, eBay etc. While working on the Princess I noticed that mine appeared to be leaking. I decided to see if I could make a new reservoir and reuse the nozzle end. Using a set of metric thread pitch gauges I was struggling to determine whether the pitch was 6mm x 0.9 or 1.0mm.

I drilled and tapped a piece of nickel rod M6 x 1.0 and tested the nozzle. It didn’t fit. I attempted to rethread it M6 x 1.0 but it then sat at a jaunty angle in the end of the bar.

Before going any further, I counter bored the unthreaded end to 8mm and reamed it. I made a press fit plug from more nickel bar, pressed it in and soldered it for good measure. Then decided to make a new nozzle using only the O ring and the needle from original.

Homemade Precision Oiler
Homemade Precision Oiler
Homemade Precision Oiler

I am really pleased with how it turned out for about an hour’s work.

More shop made tools from recycled materials – Machinists Jacks

On the tool making side of things I noted while doing some milling of small brass parts that there was a bit of deflection due to the part sticking out unsupported from the end of a collet block. I had seen video on Youtube of various people making machinist jacks to support items being machined and thought I would have a go at making some.

Although I had thought about them over time, I haven’t tried making them before because I didn’t have any suitable material but after watching how one You Tuber went about it, that gave me an idea. 

Last year, my 20+ year old mitre saw gave up the ghost and before disposing of it I salvaged what I could in the way of useful materials and fixings. The biggest chunk of useful material was the slide which carried the saw backward and forwards when making the cut. This tuned out to be thick walled tube which was 30mm OD and 20mm ID. Not ideal, initially for making screw jacks, as I don’t posses any means of making threads that big (I haven’t yet attempted any single point threading but I have just bought a couple of lathe tools for the purpose so watch this space). 

Fast forward to a few weeks ago when a friend of ours was winding down his handyman business and moving house. I asked him if he came across any bit’s of useful metal as he was sorting out ready to move, that I would take them off his hands and save a trip to the tip. He was sure there would be and a couple of days later he dropped off a carrier back full of nuts bolts and studs. In amongst the contents were a a number of cut off lengths of M16 stud, each about 4 inches long fitted with two nuts. There were also a number of M16 high tensile nuts and bolts most of them still sealed in bags (that’s how I know they are M16). A combination of these formed the basis of the jacks. I turned down four of the nuts and made them a press fit into the thick walled tube. I am not sure what the tube is made of but it really does machine well. 

Machinist’s Jack from Scrap
Machinist’s Jack from Scrap

The high tensile bolt heads were a bit tougher to turn and even harder to knurl so on the second one I didn’t attempt to knurl it. I used a carbide end mill to cut scallops and then cross drilled for a pin to allow fine tuning.

Machinist’s Jack from Scrap

I couldn’t resist adding a small brass cap to stop the pin from coming out as I wind it in and out. The two locking collars were made from another standard nut, turned, knurled and then parted into two. The standard nuts which thankfully I have most of, are so much easier to machine than the high tensile ones. Finally all the parts were cleaned with acetone and blackened with Birchwood Casey.

Eclipse Scribing Block – A cleaning test to see if my earlier efforts were a fluke.

I mentioned in the post above that I also had an Eclipse scribing block. This was a gift from a friend when he was moving and I was very grateful for it. I am a little ashamed to say that aside from using it a few times with my indicator I have done very little with it.

Having discovered the WD40/Ultrasonic Cleaning method I decided to see if it was a fluke or whether it really needed the soak in vinegar first.

Because it was a test I took a few more before and after photos

Eclipse Scribing Block Pre Clean
Eclipse Scribing Block
Eclipse Scribing Block Pre Clean
Eclipse Scribing Block Pre Clean

I put all the smaller parts in the pot of WD40 and ran it through the US cleaner for half an hour. When they came out the dirt was loose, but they were not as clean as the items that had been pre-soaked in vinegar.

On the bright side, I gave them a rub over with ScotchBrite and the dirt came away easily with almost no effort. A second run through the US cleaner had them like new.

I did the main column with WD 40 and ScotchBrite which did take a bit of effort.

Eclipse Scribing Block Restored
Eclipse Scribing Block Restored
Eclipse Scribing Block Restored

And there’s Moore… another vintage tool restoration

Hello I’m Rob and I am a tool junkie… or so it might seem.

During breakfast and morning coffee I have taken to watching YouTube videos on machining, restorations etc. while Chris catches up on the news and current affairs.

While watching one such video a gent in the states who has a superb machine shop that he inherited from his Grandfather was making an adjustable indicator holder.

The resulting tool was excellent, but as it was nearing completion I couldn’t help but notice that the design was pretty much the same as some adjustable scribing blocks that I had seen on eBay while searching for Moore and Wright tools. Sure enough a search on Moore and Wright scribing block brought up several, ranging from one with some parts missing for £10 up to pristine boxed examples that were almost £100.

I found one that was complete (if rusty in places) but unboxed, that the seller was asking £15.99 plus P&P for. I put it on watch while I browsed further. As per a number of my recent experiences, by the time that I had found a couple more at sensible (to me) prices, I had received a lower price offer from the seller of £12.99.

Offer and counter offer is one of the functions of eBay that I really like and I have used it to negotiate a better price on a number of occasions. Being a tight Yorkshireman, I decided that I didn’t want to pay more than £10 plus P&P for it but knew that if I counter offered £10 that the seller would in turn counter with £11.

So I offered £8. My thinking being that the seller would then counter with £10 and sure enough they did. Result and a happy bunny.

On a side note, I think that if you enter into negotiations like this, it is only good manners to buy the object in question although I don’t always take up the reduced price initially offered as sometimes I just put items on watch out of curiosity with no intention of buying them at any price.

This is what it looked like when it arrived

Moore and Wright Adjustable Scribing Block

I stripped it all down and put all the small parts which were rusty into a pickle jar full of white vinegar (we bought a gallon of it a while back). I left them for 24 hours and then brough them out and cleaned much of them with ScotchBrite but there were lots of small parts and springs that were either difficult to hold or lot’s of small crevices etc, to get into.

Then I recalled another video that I had watched, where a gent (again in the US) with an decent sized Ultrasonic cleaner had put various objects into small pots of different detergents including one of gasoline. These containers were then placed in the US cleaner which was part filled with water and turned on with really good results.

Another recent purchase was a 5 litre bottle of WD40 so I decanted some into a small container dropped in all the small parts and gave them a 30 minute cycle with the container surrounded by water (approx. 3/4 of the way up the container and above the level of the WD40) but no additional heat. I say no additional heat because my US cleaner has a temperature dial which goes up to 20 degrees, but even with the temperature set to zero, it still gets quite warm.

I was absolutely blown away with how clean the parts came out and the added bonus of using WD40, not only does it clean, but it doesn’t send the parts rusty like detergent or other cleaners might.

Moore and Wright Scribing Block Parts Cleaned

As you can see below there is still some pitting and general wear marks, but from any kind of distance it almost looks new.

Moore and Wright Scribing Restored
Moore and Wright Scribing Block Base Restored
Moore and Wright Scribing Block Base Restored

Now as I mentioned at the beginning the plan is to use this as a dial indictor holder rather than a scribing block as I already have a nice Eclipse Scribing block that a friend gave me. More on that in another post.

This is the finished and reassembled tool fitted with a dial indicator.

Moore and Wright Scribing Block Restored

More on Callipers, or Should that be Moore

I wasn’t really sure where to post this only that I didn’t want to distract further from Adrian’s excellent scratch build with it.

Further to my post here on buying a set of Moore and Wright odd leg/Jenny Callipers second hand via eBay the next day I received a second reduced price offer on a selection of four pairs of Moore and Wright Firm Jointed Callipers for £10 plus postage so in for a penny etc. I bought them.

They arrived today and although not in quite as good a condition as the first pair that I bought they have none the less cleaned up nicely and if I spent a bit more time on them I have no doubt that I could get them back to being almost pristine.

Moore and Wright Calipers

Although they were listed as two pairs of odd leg and two pairs of external callipers. One of them had had the legs reversed and is, on the basis of where the writing is positioned in relation to the other pairs, an internal set giving me a nice range for very little investment in them.

I have included below the first pair that I bought now that they have been cleaned up. So quite unintentionally I now have a three pairs of odd legs all of which are different sizes. So I can have one pair for marking out on the lathe, a pair for the mill and a pair for the bench. 

Moore and Wright Calipers

Having seen them all together I don’t think that I will be able to resist having a further go at cleaning/rubbing them down to try to make them all as good as I can.

Odd Leg/Jenny Callipers

A recent post on scratch building a loco over on Western Thunder highlighted some of the basic tools used for scratch building. The gent in question (Adrian) posted a photo of the tools laid out on his bench. They were the usual scribe, 6in rule, dividers, set square and, a pair of odd leg callipers.

Now I am sure that I am not alone in my lazy habit of using expensive digital/analogue measuring callipers for scribing my marking out when machining…

A quick look on the web revealed that I could get some Chinese odd leg callipers for under a tenner but already possessing a set of Chinese (or indeed they might be Indian) cheap callipers which are crude to say the least I thought I would have a look on eBay for some second hand named brand alternatives to see what was/is available. Now one of my favourite Sheffield made brands are Moore and Wright so I started there.

Searching Moore and Wright odd leg callipers brought up quite a selection even some new ones. Many of the cheaper end of the buy it now examples were simply two pieces with one leg bent and the other sharpened. Having seen Adrian’s set I rather fancied a set that had a separate scribe pin. I was a bit short of time so I put a couple on watch and returned to them the day after. As it turned out it was the same seller selling both of them and overnight I had received Offers on them. The offered reduction was only a couple of quid but it meant that the better of the two pairs that I was watching came in at £10 posted.

Moore & Wright Odd Leg Calipers
Moore & Wright Odd Leg Calipers

This is what I got for my tenner. A rub over with Scotch Brite and WD40 and they will be as good as new. I am well pleased with them and will enjoy using them for many years to come

The arrow alongside the date leads me to think that they are ex military

Each time I use them I will think of Adrian, and his unbeknownst kick up the pants.

This would have been an edit but I forgot to click post reply before applying the Scotch Brite. They have cleaned up as I imagined and while doing so I found a couple of small dings which I smoothed out with a diamond stone so they are now as good as they can get.

Back on the Recycling Trail

I did a little more potentially useful recycling today. Earlier this week I discovered a brand new round file which needed a handle. The very next day we received our grocery order and in it was a new dish washing brush which meant the old one was being discarded as being worn out. As I was about to put it in the recycle box I wondered if the handle was solid as an idea was forming. I popped it in the workshop and this morning I had 10 minutes to saw the remains of the brush head off to see if the handle was solid.

Having determined that it was solid, I measured the file tang and cut the brush handle to length leaving the comfort grip. I drilled out the cut end to accept the file and a few bashes with a rubber mallet later and I now have a file that is really comfortable to use.
I have to admit that the colour is not great but I am not too fussed about that.

Modified by CombineZP

Drill Chuck Key Comfort Handles

This may not be as relevant to some in these days of keyless chucks but here goes.

I have got into the habit of watching Youtube videos on my phone while having coffee, usually on lathes or machining of some sort. During one such video yesterday a guy in the US had made comfort handles for for drill chuck keys and when he explained why it struck a chord.

Today while at the lathe making return crank bushes for the Princess I decided to have a go at a handle for the chuck key for the drill chuck that I use on both my lathe and mill.

Chuck Key Handle
Chuck Key Handle

Really quick to make and it doesn’t need a lathe to do it. A Drill and a file would suffice. I made it so the handle was a tight interference fit and I did such a good job that I had to drill a 1mm hole in the end to let the compressed air out to allow it to push into the bottom of the main hole in the handle. It got quite a bit of use while making the bushes so this evening and it was so much more comfortable to use that I made a second one for the much smaller chuck key for my Proxxon Mini Pillar Drill

Chuck Key Handle

Both handles are made from offcuts of Delrin rod that I had in stock but they could be made from pretty much anything. I had eyed up wooden dowel, aluminium bar and brass rod before remembering the Delrin.

Cheap and Cheerful Home Made Nut Spinners

For those of you not wishing to spend a packet on BA nut spinners from Markits et,al a chance conversation with a friend brough back a memory of a much missed GOG Member whom I have referred to in the past David Smith (known on various forums as DLOS). He was really a model engineer and he had mention in a posting a few years ago that he had made BA nut spinners from appropriately sized caps screws using the hex head as the socket.

Having a spare couple of hours last night I rummaged through my screw box and found that an M4 and M5 cap head screws were just right for 8 and 10 BA and a couple of grub screws suited 12 and 14BA.

Home made Slim Line Nut spinners 8-10-12-14 BA

Although I used the lathe they could be made by anyone with the ability to drill and tap metric threads. I did turn down the heads of the cap screws but again nothing that couldn’t be achieved by putting it in a drill chuck and applying a file.

A tip worth mentioning: If you use grub screws for any of them, in order to get enough threads to engage the grub screw, you need to drill the hole a bit deeper. This means that the head of the grub screw wont stay at the end. My solution was, once threaded, I screwed the grub screw in as far as it would go and then with a bit of brass rod I measured how far in the head of the grub screw was from the end (1.5mm and 4.5mm respectively in my case).

I then cut a couple of short lengths of brass rod that would slip inside the threads (2mm I think I used) This allows you to tighten the grub screws against the bottom of the hole while the head is level with the end. I was planning on Loctite-ing them but I don’t think that they need it.

The handle parts were made from a length of bent 6.35mm brass bar which equates to a 1/4 inch (I must have bought it as quarter inch but any suitable sized bar would do. Hopefully it’s the last bent piece in my stocks as there is nothing more irritating than trying to tun something that you have to lose half it’s thickness before you get it to run concentric.
It’s not visible in the photo but the bend in the bar meant that the grooves look a bit like Zebra stripes, in that go they go thick then thin as the bar flexed away from the cutting tool as I turned them. You don’t need them for the tool to be functional but I can’t help messing.

Recycled Allen Key for locking/unlocking the Sieg Mini Mill table locks

I know that there is at least one other reader with a similar Milling machine to mine so I thought that this might be worth sharing.

For many milling operations, the accuracy of the work is improved if you lock the table in one or both axis. The problem with doing that is access, particularly on the Y axis. Locking the table is done by means of a cap screw which when tightened nips the gibs and prevents the table from moving in that axis while you work. These are located in the mid point of each axis. The Y axis one being under the table at the right hand side and directly in line with the hand wheel. There isn’t a lot of room in the there and for me at least at best I get my knuckles covered in grease at worst I leave skin behind… I do have a set of long T handled Allen Keys but the T bit is too long and it has to be put in at an angle to clear the hand wheel.

While watching a video where someone else was struggling to tighten the mill table down it occurred to me that I needed to make something with a straight shank that was thick enough to grip and turn

I initially planned to use brass or acetal but while rummaging in my tub of Allen keys looking for one that I could cut down I found and old cheapo centre punch with a knurled grip. It was so cheapo that at best only the tip must have been hardened because the tip was totally mashed up and cutting the end off, facing it and drilling it out on the lathe was no effort at all. Once drilled I ground a slight chamfer on one end of the stub of Allen key and bashed it into the punch handle.

Recycled Allen Key

Now I have the perfect tool. It fit’s under the mill table and allows me to lock/unlock the mill table with minimal effort. I had thought of cross drilling it to add a small cross bar but I don’t think I need it.

Shop Made Machinists Hammer

A while ago when making the improvements to the tail stock of the Unimat, I mentioned that I planned to make a machinists hammer.

Well, I made a start and ,machined up the body of the head the screw in faces, and the shaft but hadn’t done anything about the handle by the time I sold the Unimat.

Primarily this was because I had struggled to thread the 8mm stainless rod that I used for the shaft and was awaiting delivery of a new set of metric taps and dies to complete it. The taps and dies duly arrived but by then I was on with other things so it was being used just with a the bare rod as a handle. I had managed to thread the end that fits into the head it was the handle end that I had struggles with. About 3 weeks or so ago I got around to threading the handle end of the shaft but was undecided as to what to make the handle from. I had a choice of some 16mm diameter aluminium rod or some of the acetal rod that I had made the faces from. which is just over 20mm diameter. In the end I opted for the acetal. but it wasn’t until yesterday that I got my finger out and made the handle.

Having drilled and tapped it 8mm. Instead of knurling the acetal rod to create the grip, I decided to turn concave grooves using a HSS tool bit that I had ground into a curved end but hadn’t tried out on anything.

Once that was done it was just a case of fitting them together. In the end I had to cut a few threads of ether end to ensure that no threads were visible where the shaft enters the head or handle as I hadn’t really thought too much about how much thread I was creating versus how deep I could actually tap each piece.

Home Ground HSS Cutting Tool

Aside from regrinding a few tools to sharpen them, this is my first real go at grinding a tool from a blank to create a particular shape. My plan with this one is to have a go at turning a chimney at some point.

Home Ground HSS Cutting tool
Shop made machinists Hammer

Once I screwed the faces onto the head and the handle onto the shaft I couldn’t get them off again without risking marking them up so I wasn’t able to take any photos of it further disassembled.

Shop made machinists Hammer

This is the finished hammer which has turned out rather better than I had hoped when I started out. It’s main function will be to ensure that materials are seated properly in the mill vice of lathe chuck but I am sue that I will find other uses for non marking brute force….

Shop Made Tail Stock Locking clamp for the Unimat III

I mentioned in my Parting tool upgrade post that I planned to upgrade the locking clamp for the tailstock too.
Like many locking clamps on the Unimat III the locking clamp for the tail stock is an M6 cap screw. It being tucked down the side of the tail stock body it isn’t always convenient to get to. Watching the videos from the GOG virtual shows done by the late David Smith (DLOS) on workshop practice I noted that he had done a similar upgrade and it prompted me to think about it. I finally go to it.
As luck would have it I have a small stock of 50mm stainless M6 cap screws. These are only threaded for part of their length so I started by threading one of them along it’s entire length. Not an easy task in stainless but I got there. Next I cut of the head and cut it approximately to length. 
Then I drilled and tapped a short length of 16mm aluminium bar M6 and turned a 20% taper on the closed end. Having tried to fit it all together so that I could work out the handle length I realised that I had it too tall and it wouldn’t screw past the body of the tail stock. I parted off 5mm and that cured the problem. I screwed it on hand tight an marked where the handle was gong to be and had to change plans again.
My initial idea was to use another M6 screw for the handle and make a knob similar to the pinch boss to fit on the end. My test run proved that there just wasn’t enough room for any kind of knob so I was pondering what I might do when I remembered that I had a short length of steel bar in my tool box that I had had for years and it usually found use as a drift so was a little battered on the ends.
I faced one end off and turned it down to 5.85mm to thread M6 again it being stainless, made this a bit of fun but once I got it started it wasn’t as hard as threading the screw. Then I decided to taper the rest of it to make a handle shape so I centre drilled the threaded end and used a live centre to support it while I turned the taper. After initially completely forgetting that I needed to turn the topside feed not the carriage feed I ended up with the handle below which I was quite pleased with.

Shop made Tail Stock Clamp Handle.

Having cross drilled the pinch boss I assembled it all and it looks like this

Shop made Tail Stock clamp


This is the unlocked position and a quarter turn locks it

Shop made Tail Stock clamp

Carried away by this success I have ordered some more 8mm stainless rod to make another to replace  the cap screw on the quill lock.

Shop Made Parting Tool fixture

3D drawing has been a bit of a distraction from the other things that life has thrown my way recently but I also made a small upgrade to my parting tool holder for the Unimat.

Due it small size I had to buy a mini parting blade and this is what it looks like below

Parting tool as supplied

The bit that’s supposed to hold the blade and keep it from moving is this bit, which is for all the world like a bent washer.

Flimsy Clamping fixture

After parting a few items off I noted that on some of them the back of the part was actually convex because the cutting force had bent the “washer” and allowed the parting tool to move to one side as it was cutting.
Having bought my long length of steel from Wickes I decided that I would look at making something a little sturdier.

This is what I came up with.

Shop made clamping fixture

The slot is wider than the blade (1.45mm) because my smallest milling cutter at present is 3mm but I do have some brass bar that will fit in the remaining slot should I need to take out any slack.

Here it is fitted.

Shop made parting tool clamping fixture

There is a small shim in between the fixture and the tool holder which helps apply an even pressure. The fixture is thick enough not to bend under pressure and long enough to hold the blade inline with the tool holder without being able to twist while cutting.

Next I plan to make a locking handle for my tail stock. It currently locks via a cap head M6 screw which isn’t always very convenient.