I have spent the last week or so fixing a number of mistakes that I made back when I didn’t know any better. For example, I realised when trying to fit the wheels that I had assembled the Premier coupling rods as a pair rather than handed, so one side only fit inside out. At the back of the workbench, I found an old pin punch. I popped it in the lathe and turned a small spigot on the end, to allow me to carefully pop out the rivets and swap the sections of rod around.

Once corrected I was happy to find that the rods ran smoothly in both directions without any sign of binding.

(As an aside I do like the built in motor restraint which is a nice bit of design work.)
The next bit of corrective action took most of a day to sort out. I had previously bent and fitted the two steam pipe sections that fit between the grease separator and the exhaust steam injector. These are made from 3.1mm copper rod which takes a bit of working to shape. Fast forward a few years and the grease separator casting had come adrift from its mounting pad and I hadn’t actually secured the front section of pipe. It was just pressed into the front flange of the grease separator casting. Without paying much attention I soldered the grease separator casting back in place and moved on to more of the motion parts.
While working on these I thought that it might be wise to fit the wheels and check that the Premier coupling rods matched the MOK wheel base and that I had a smooth-running chassis. It was at this point that I realised that the route of the steam pipe prevented the rear axle from moving through its full travel once the motor was fitted – The rear axle sat a good millimetre higher than the front axles. So, I removed the pipe (and the castings at either end) adjusted them and refitted to find that the pipe now hit the tyre on the rear wheel.
At this point I stopped refitting the castings and just kept adjusting the pipe bends. I did much of this with the aid of my vice, a thick-walled steel tube filled with lead and a white rubber mallet. I also made use of the “Markits” BA nut spinner set for making the tight tweaks to the very end bends after finding that the 8BA size just fit over the copper rod. I spent a couple of hours on Christmas Eve and around six hours yesterday before I finally got it to fit in place and clear both rear wheel and allow full vertical movement of the gearbox.
In reality once I come to set the ride height, the vertical movement of the gearbox may be less of an issue but better safe than sorry.












































































